Case Study: RMR® – BP Egypt
Learn how Enhanced Drilling provided Riserless Mud Recovery (RMR®) services to BP Egypt in 2008 so that a deep 22”
surface casing could be set, despite a weak conductor.
- CHALLENGE: A weak conductor made it difficult to install service casing at about 1,085m (3,560ft).
- SOLUTION: Standard RMR® equipment was modified for this
operation, so that a deep 22” surface casing could be set, despite the weak conductor. - RESULTS: With the 22” casing at this depth, there was no need to use the 16” liner, saving 10-20 days rig time, or $5m-10m (based on previous wells).